Today, the programmers split into two teams. Austin and Maxim is working on the PID and Peter is testing the sensors.
The engineering team is also working on various projects. Rory is working on SolidWorks to scale the entire robot. Ethan, Ryan, and Junha are fixing up some malfunctions from the previous meeting. They are adding spacers to the side thats closest to the motor so the sproket won’t hit the nut thats attatched to the motor. Erina and Max are adjusting the holes on metal parts to make them bigger, since the CNC machine is broken.